General Late Model Tech All LM technical discussions except GTO, G8 and TA here! |
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02-27-2022, 06:29 PM
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Ultimate Warrior
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Join Date: May 2004
Location: nampa id
Posts: 1,122
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Idle problems in 5.0 99 ford
So I seem to have an idling problem in my 5.0 when the motor starts up motor starts shaking like it's missing but it clears up after 12 1300 RPMs and you give it gas but when it comes back down to idle it starts sputtering and trying to stall again we have changed everything from EGR valves cam sensors checked every fuel injector did voltage readings on everything compression check and it still has the same problem . We also checked the fuel pressure fuel filters and everything is okay
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1970 firebird, 468, e heads,
Last edited by jamaca85; 02-27-2022 at 06:36 PM.
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02-27-2022, 06:43 PM
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Senior Chief
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Join Date: Jan 2022
Location: Michigan
Posts: 283
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Vacuum leak?
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02-27-2022, 06:47 PM
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Ultimate Warrior
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Join Date: May 2004
Location: nampa id
Posts: 1,122
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We already covered that no vacuum leaks actually replaced all the vacuum lines on the motor but thanks
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1970 firebird, 468, e heads,
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02-27-2022, 07:09 PM
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Senior Chief
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Join Date: Nov 2007
Posts: 457
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Wasn’t the last year for 5.0 in 95?
A couple ideas…. have you verified your timing? Have you checked the idle air bypass valve for proper operation? They can get plugged up. Also mass airflow meter can have issues….
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02-27-2022, 07:47 PM
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Ultimate Warrior
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Join Date: May 2004
Location: nampa id
Posts: 1,122
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yes we have checked both..the idle valve is working and not plugged, mass air sensor has been replaced...thats whats so weird about it. we have gone from gas tank to injectors still has the issue. ran fine till he parked it for a week then issue started. the odd thing is it hasnt thrown no codes
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1970 firebird, 468, e heads,
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02-28-2022, 01:49 PM
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Ultimate Warrior
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Join Date: Jun 2011
Location: USA
Posts: 2,559
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Did you replace the battery or disconnect it recently? If so it may need to relearn the idle strategy and may require about 20 key starts.
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1978 Black & Gold T/A [complete 70 Ram Air III (carb to pan) PQ and 12 bolt], fully loaded, deluxe, WS6, T-Top car - 1972 Formula 455HO Ram Air numbers matching Julep Green - 1971 T/A 455, 320 CFM Eheads, RP cam, Doug's headers, Fuel injection, TKX 5 Spd. 12 Bolt 3.73, 4 wheel disc. All A/C cars
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03-01-2022, 07:45 PM
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Ultimate Warrior
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Join Date: May 2004
Location: nampa id
Posts: 1,122
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thanks i will ask him
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1970 firebird, 468, e heads,
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03-01-2022, 08:51 PM
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Ultimate Warrior
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Join Date: May 2004
Location: nampa id
Posts: 1,122
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Yeah I'm hoping that somebody has run into this issue with the same symptoms with with no check engine light and has solved it
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1970 firebird, 468, e heads,
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03-01-2022, 10:11 PM
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Ultimate Warrior
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Join Date: May 2018
Location: Nebraska City, Nebraska
Posts: 1,962
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That is a pretty common problem on fords that era. Been a while since I worked on those but if I recall correct the issue is up by the throttle body at the AIC. It requires disassembly and cleaning. There should be how to videos on you tube. Look up Ford idle air control valve. It causes a big dead spot coming off idle if it doesn’t work or is slow. If it is bad a check engine light will come on. If it is gummed up and slow the check engine light will likely not come on.
Last edited by Jay S; 03-01-2022 at 10:21 PM.
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05-25-2022, 06:41 PM
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Ultimate Warrior
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Join Date: Jul 2004
Location: Mt. Laurel NJ, now Melbourne, FL
Posts: 1,390
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Stupid question, is there a K&N filter on there? The reason I ask, I worked at a Ford dealer for years and the open K&N filters would disturb the MAF sensor because of the turbulence from the radiator fan. If there is, try installing the factory filter box and see if it corrects the issue. You could put cardboard to block the wind turbulence to test it.
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06-01-2022, 08:24 AM
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Ultimate Warrior
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Join Date: Jul 2004
Location: Mt. Laurel NJ, now Melbourne, FL
Posts: 1,390
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What wound up being the problem?
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